Phase 1 research identified a two-step refining train, acid leaching of AMD precipitate feed followed by solvent extraction (SX), to produce a 2% TREE product. For the Phase 2 bench scale system, the objective was to get the acid leaching step to operate in batch-mode with sufficient storage capacity to feed an aqueous, enriched REE liquor to a pilot SX plant operating in continuous-mode at a feed rate capable of producing 3 g/hr 2% TREE. Important process variables included feed rate, extractant makeup, flowsheet configuration, and stripping conditions. Operating parameters were optimized through a feedback-capable SCADA system configured for the SX bench scale plant. These conditions were met and exceeded. TREE grades approaching 90% were produced while our Techno-Economic Assessment indicated highly favorable economic returns. The project led to the design of a pilot facility for producing roughly 500 kg/TREE/year. That plant is now in the procurement stage with constructed expected to begin in late 2020.